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E L E C T R I C I T Y F O R A B E T T E R L I F E

PENINGKATAN PENGENDALIAN PROSES BISNIS UNTUK MENCAPAI WORLD CLASS SERVICES. RAKOR TW-IV 2013, LAMPUNG 8-10 JANUARI 2014. E L E C T R I C I T Y F O R A B E T T E R L I F E. PRODUKSI BERDASARKAN TIPE BAHAN BAKAR (FUEL-MIX). HPP : 1.138,- Rp/KWH. HPP : 1.209,- Rp/KWH. HPP : 1.112,- Rp/KWH.

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E L E C T R I C I T Y F O R A B E T T E R L I F E

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  1. PENINGKATAN PENGENDALIAN PROSES BISNIS UNTUK MENCAPAI WORLD CLASS SERVICES RAKOR TW-IV 2013, LAMPUNG 8-10 JANUARI 2014 E L E C T R I C I T Y F O R A B E T T E R L I F E

  2. PRODUKSI BERDASARKAN TIPE BAHAN BAKAR (FUEL-MIX) HPP : 1.138,- Rp/KWH HPP : 1.209,- Rp/KWH HPP : 1.112,- Rp/KWH PLTD Payoselincah OFF Mulai 1 April 2014 HPP : 1.047,- Rp/KWH

  3. OVERALL EFFECTIVENESS EQUIPMENT 87,4% EFOR

  4. 0 Analisa Pareto Lost OutputPLTD/G Sektor Jambi Periode Semester 1 2013(Januari - Juni) Periode Semester 1 2013(Januari - Juni) Lost Output Sektor Jambi (Tidak termasuk Sewa) Reasons for Force DeratedPLTD&G 0,11 Total Potensi PLTD&G 441,12 56.2 FO &FD PLTG BH 2 Temp.Oil header High 30,9 (51,1%) Crack 1st Stage nozzle and Temp.Spread TRIP Total 11,96 FO &FD PLTD 15,9 (20 %) High temperarture exhaust Oli Leackeg in Pipe SOGAV Fault Total FO & FD PLTG BH 1 11,40 (19,1 %) * Note: Gap yang berwarna Kuning telah diselesaikan TemperatureSpread Trip(3x) Total

  5. 0 Analisa Pareto Lost OutputPLTD/G Sektor Jambi Periode Semester 1 2013(Januari - Juni) Periode Semester 2 2013 (Juli- Desember) Lost Output Sektor Jambi (Tidak termasuk Sewa) Lost Output Sektor Jambi (Tidak termasuk Sewa) Total Potensi PLTD&G 441,12 404,8 Total Potensi PLTD&G 56.2 9,1 FO &FD PLTG BH 2 FD&FO PLTG BH 2 30,9 (51,1%) 1,4 3,8 FO &FD PLTD 15,9 (20 %) FD & FO PLTD FO & FD PLTG BH 1 11,40 (19,1 %) 3,9 FD&FO PLTG BH 1 *Angka dalam satuan GWH

  6. 89,61% OVERALL EFFECTIVENESS EQUIPMENT 2014 Strategi : 1. Mengurangi waktu masa pemeliharan periodik 2. Penggantian Filter Online

  7. KINERJA PROSES

  8. PROGRAM PENDUKUNG 2014 PROGRAM (PENDUKUNG) TW-1 2014 PT.PLN (Persero) Sektor Pembangkitan Jambi GUDANG ONLINE ® Sistim Informasi Gudang DATABASE (SERVER) IMAP – MAXIMO™ OLIFE ® DASHBOARD Sistim Informasi Outage Manegement dan lifetime hot section gas turbine. Computerize maintenence management system. E-LOGSHEET ®DASHBOARD EFFICIENCY® DASHBOARD E-LOGSHEET ® FORM Sistim Informasi Heat rate dan Efficiency PembangkitPLTG Informasi data operasi dan pengusahaan pembangkit Formulir data operasi

  9. WORKPLAN Aktivitassesuaijadwal Rencana 2014 Aktivitas proyek selesai

  10. NILAI KINERJA (SUMMARY)

  11. PROGRAM KERJA 2014

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